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Some more progress and, SPOILER ALERT, the motor is in!

A little over a month ago there was the first progress update in two years. Because of the pandemic I had the time to go up to Sacramento regularly and get moving the project along; Stu welcomed this because he didn’t have time to do it yet wanted to see things go forward. The goal was for me to go up at least once a week, which I’ve been able to do since the last post.

Reassembly presents a strange dichotomy. It is sometimes simultaneously enthralling and frustrating. It is enthralling to reassemble a car that was touched by the hands of God, the Alpina factory, seeing what they did—both sophisticated and, occasionally, somewhat primitive.

But the challenge of finding the parts to reassemble the car is frustrating. The disassembly was haphazard and parts show up in the strangest places in the shop, others missing or found after I’ve ordered new ones. At times it seems I’m spending more time searching the internet for little bits here and there than reassembling the car. On top of that, some of the parts I collected 4 years ago turned out to be the wrong ones (and can’t be returned now) or are just missing. On top of that, there’s the steep learning curve of trying to assemble a car you didn’t take apart.

The door locks are great example. They were taken out for painting and the original gaskets were nowhere to be found—probably they deteriorated and were not reusable—and new ones needed to be ordered. New ones were sourced from a local BMW dealer, but they didn’t work—they were round without indents to follow the contours of the lock body. Although the right part number, BMW apparently has consolidated those gaskets with ones from other cars and the “right” part (according to BMW) didn’t fit my car. A search on eBay found the New Old Stock ones that would work but they were in Greece (gotta love the internet!). The vendor had great feedback and several other BMW parts for sale so I clicked buy.

Four weeks later DHL delivered the gaskets and I finally had everything needed to put in the door locks. Getting the lock cylinder into the door was a trick, at least for someone like me who has never done it before. I started with the passenger side. The cylinder seemingly did not fit into the hole in the door; after fruitlessly trying to wiggling it in, I got more and more forceful, pushing it and then finally I held it centered on the hole and hit it with the palm of my hand. It barely went in and fell out as soon as I touched it. But, progress (however slight). A small hammer and gentle taps and it was in, but not by much—maybe a quarter-inch. Hit it a little harder and it went further in. Even harder and it was halfway in. Consistent gentle taps slowly morphed into firmer hits and it was getting closer and closer; it took a mere half an hour to get it firmly planted in the door. Learning how hard I could hit it took time; the fit was so tight it needed some serious force but I didn’t want to wack it too hard and damage the door. Then it took me 15 minutes to figure out how to attach little arm on the back of the cylinder to the lock; adding to the frustration was working in a tight space with no good line-of-sight. But, I figured out what parts of the door innards to disassemble to get room and sight; once I did, it was an easy job. The passenger side took 45 minutes (most of that being the learning curve), but the second one was finished in less than ten minutes. Knowledge is a powerful tool!

Another challenge was figuring out how the bundle of wires was supposed to routed through the engine compartment. I looked at the harness, which had an ugly re-wrap in electrical tape, and it was not at all apparent how to get from the fusebox to the headlights and horns. I inquired on the FaceBook e21 group and I found someone who restored a similar C1 2.3 (really, any e21 would have been fine, but it was great to find someone who did such a great job and documented it with photos). He sent pictures of his wiring and I was in business. I re-wrapped the harness in friction tape and routed it through the engine compartment.

With the wiring in, next was the bumpers. They had been sitting around the shop literally collecting dust. I washed them off and then installed them.

Then I installed the horns and lights and then grills.

Then air dam. And talk about collecting dust! It looked like it had been painted some weird animal print pattern, but I washed it and it was good to go.

Putting the air dam on the car was one of the interesting archaeological parts of the restoration. The air dam has brake cooling ducts but behind the ducts on a stock body is the lower valance. So the boys at Buchloe cut a rectangle out of the valance to allow the air to flow to the brakes. Those cuts were uneven and kind of primitive. Honestly, they looked like something I would do in my garage!

And sometimes it’s just fun cleaning things up and making them look spiffy; the hood latches were old and rusty, so into the media blaster they went. Quickly they were cleaned up and sprayed with lacquer. A serious improvement.

A project like this has a ton of small things that need to be done, like running the wire back through the small channels on the inside of the trunk lid. Fitting the wiring through those channel can be a challenge, but patience and persistence pay off.

But it also has some significant challenges. One was the metal brake line to the caliper on the front passenger side. The original one was bent, weak, and just ugly.

<PICs of old brake line>

When you buy brake line, BMW provides a straight piece of brake line that you have to bend to fit. What really makes it a challenge is that the line takes a very circuitous route from the master to the caliper and the original line was bent when it was taken out and it couldn’t be used as a template. I got a pic of the route, which was helpful but still not specific enough. We went to a junk yard and were gifted a template (the old rusted line from a carcass of a 320i). Using a template made mimicking the route much easier and the finished product looks as good as from the factory.

After that, the rest of the brake system—booster, new master cylinder, and reservoir—get installed. The brake master was one of those problems with the delayed project. Four years ago I ordered a new one but when I went to install it, the fittings where the brakes lines screwed in were in the wrong places. Too late to return it, I had to get another new one, this one fitting just right.

With most of the work done to the engine compartment, it was time to drop-in the motor. Putting in the motor was pretty straight-forward and two nuts later, it was part of the car again.

With the long block in, building it up to be a working motor was up next. The old thermostat manifold was not in great shape and need some heat to take it apart.

The fuel injection is up next but offers some challenges. With the bigger displacement, the stock 323i/C1 fuel injection won’t flow enough fuel. Four years ago, I bought the necessary parts (I’ll describe those in a future post) but Stu swears he doesn’t have them and I can’t find them in my parts stash. Luckily, Stu had similar ones in his parts stash and we should, soon, be good to go on that front…..

Progress, finally…

It’s been over two years since my last blog update and four years to the day (November 1) since I proudly posted on FaceBook that I bought this car, my first real Alpina. I say first because I now also own a 1981 B7 turbo e12 (www.alpinab7.com). I bought the B7 largely because it is just such a cool car; but, I also partly bought it because this project had stalled to a point that I wanted a cool vintage that I could drive while trying to get the e21 back in on the road.

The pandemic has helped many car enthusiasts, including me, by giving them time to wrench on their project car. Happily, most (if not all) of the attention was focused on getting the B7 in better shape. The car was not well-cared for over the years and, while it was a decent driver-condition car, it needed a bunch of TLC. And the pandemic kept me at home where I could order parts on-line and wrench on the car, giving it the much-needed attention.

The pandemic, however, did not help this project. Stu’s shop was negatively effected by the pandemic, losing mechanics (not because the virus) and forcing him to focus on his day-to-day business and not follies like restoring old Alpinas. He does, after all, have a shop to run, customers to keep happy and on the road, and bills to pay with normal, more profitable work. So, the C1 was the neglected red-haired step child. The C1 had been painted but not reassembled (Stu sold his body shop and the car was moved to the main shop, but mostly sat, waiting for Stu to have free time to put it back together).

I got to a certain point with the B7—sort of a go big or go home point, where the car should just be driven as-is or take a big step in restoration. Regardless of the path chosen, I passed the point of tinkering on it in my garage, as going “big” meant it taking it back to the turbo specialists who would make the fuel injection more reliable—a job way, way above my pay-grade. At those cross-roads with the B7, I turned my attention to the C1, which began with a call to Stu.

I figured the best way to get this project going forward was for me to go up to Sacramento and start assembling the car myself. Before I could make that suggestion Stu says “you should come up here and do the easier stuff yourself and help me do the harder stuff.” I jumped at it and we made a plan. That was a few weeks back and I’ve gone up three times (so far) in the past two weeks.

Our first job was putting the “new” dash in the car. The original dash had been sent to Just Dashes for repairs, which looked great but the fit was tight. With me, Stu, and his 18-year-old shop helper pushing and pulling, we got it in.

Stu worked on installing the new the headliner.

The three of us put in the windshield.

And I bolted up the valance panel.

Much of my time was spent organizing the parts taken off in disassembly, which took a good amount of time. The guys at the body shop took it apart assuming they’d be putting it back together immediately so the disassembly was not organized in anticipation of a multi-year project. Finding everything more than two years later was (and continues to be) a challenge, but not an insurmountable one. While searching for unlabeled, haphazardly placed parts is not particularly fun, the project is: all my past restorations have been mechanical or interior work. Reassembling a car striped for paint is a new experience. And a good portion of the satisfaction of a project for me is the connection, the bond, one gets with a car when restoring it. And I’m feeling a special bond with his project, with its new (to me) challenges; challenges akin to building a car anew.

Our plan is for me to keep going up to Sacramento until we get the car to a point that it can be put on the back of a trailer, driven back down to my house where I’ll finish the work.

Final Motor Specs

As described in the last post, the motor build is mostly completed. There are a few weird odds-and-ends yet to be done, like a drill and tap for a bolt to secure warm-up regulator to the block and such – nothing major. But I realized that the final build specifications were never discussed fully. So here’s a chart and explanation of my build, comparing it to stock BMW and the Alpina build.

Virtually every decision-point was vetted. Twenty-eight hundred cc displacement was chosen because I wanted to use a turbo-diesel crank (it’s a very stout crack, able to withstand the high pressures of the diesel motor) and I always kinda liked the e30 c2 2.7, based on the same crank and big bore. The pistons were an easy decision, given the crank and desire to get at least 2700cc. I didn’t feel the need for a much bigger bore and knew that several folks had successfully used a 86 mm bore on the stock 325i M20 block.

The rods were a compromise. Because the pistons were custom, I could use virtually any BMW rod that fit the crank. If I used stock BMW rods, I would spend money buying them, testing and refreshing them, and lightening and balancing them. If I went with proven, USA forged rods like Carrillo or such I’d spend a fortune. For the same price as used rods plus machine shop work, however, I could get forged Chinese rods that were finished in the USA by a reputable shop. That is just what I did, with 135mm rods from Molnar Technologies. Tom Molnar was the Metallurgist and engineer for Oliver Rods and Cranks for over 20 years; he was the founder of K-1 Technologies and recently started his own shop. I was confident with that background that my compromise rods were built by someone with the necessary know-how.

The Schrick 272 was also a compromise camshaft, but for different reasons. Retaining the Bosch K-Jet fuel injection was the limiting factor. From what I’ve been told, the flap in the air-fuel meter is sensitive to pressure changes in the intake plenum and a higher-duration cam will create too much pressure change for the K-Jet fuel injection. Normally, with the increased displacement, I would build in more cam – and while the Schrick 272 is a “bigger” cam than the stock Alpina 268, it is not monumentally so. Obviously, it’s only 4 degrees more duration than the Alpina cam and 12 more than BMW. In the faux A4S I built, for example, I had 2.2 liters of displacement (S14 crank in stock M10 block) and a Schrick 304. The 304 has significantly more duration than the 264 degree stock M10 cam and is usually thought to be too much cam for the street, with high horsepower but little bottom-end power. But the increased displacement made up for that and the motor was actually very docile and flexible – lots of horsepower but the increased cubic inches (or centimeters, as the case may be) gave it lots of low-end torque. If I could have done that here, I would have. But no such luck and the 272 was the most duration I could comfortably get while retaining the stock(ish) K-Jet fuel injection.

The M20B25 block was chosen simply for convenience – there are a ton of them available and but for the drill-and-tap for warm-up regulator, there are no practical differences. The 885 head is said to flow best of the available M20 heads, so that choice was simple too. The head and intake plenum were mildly ported and matched.

I guestimate the motor to put out about 200 horsepower and 185 foot-pounds of torque. Both numbers represent a gain of 30 horsepower and foot-pounds. The horsepower is an educated guess, starting at the Alpina 170 mark for the 2.3 liter C1 motor and then comparing to the Alpina B6 2.8, which has a tad less displacement (2788 v. 2823). The B6 motor puts out 200 or 218, depending on fuel injection and cam. The Pierburg version of the B6, with an airflow meter similar to the K-Jet and a 260 degree cam, puts out 200. The Bosch L-Jet version with a 280 degree cam, puts out 218. Mine is probably somewhere in between but 200 should be a safe number, given the displacement, cam, compression ratio and fuel injection. (Note that Alpina used considerably less cam duration for fuel injection similar to mine.)

For torque I used the B6 2.8 as a reference point as well. The early B6 motor put out 182 and the later 195. Mine should be in the middle as well but 185 is a safe number.

If these numbers are right, I will be getting B6 performance essentially with weight savings of 57 pounds – all at the nose. (The M20 weight is 258 lbs while the M30 is 315 pounds.) That’s not bad!

A comparison of the C1 and B6 specs can be found here: http://www.bmwe21.net/?page_id=301

The Motor, completed. Sort of.

The last post – Death by a thousand delays – ended with more parts missing and some health issues for me, causing another delay. But, it turned out the time off from work allowed me to focus on the motor. And I got it out the door and off to Sacramento, to be tinkered with a tad and then, hopefully soon, dropped in the car.

With the washers for the head bolts sourced, I was able to finally install the head.

And then the drive belt and the pulleys.

Then the oil pan was ready to go on.

And then the rest of the rotating mass and the front covers.

Once the motor was assembled, I was able to take some time to appreciate the machine work. Here, the intake ports were gasket matched to the intake manifold.

And visa-versa for the intake manifold.

I made plans with Stu for him to bring his X5 down to my house and pick up the motor and the various parts. That meant next up for me was organizing the other parts. Got a couple or four bins of parts together.

And put the motor on the cherry picker.

Stu came and picked up the motor late one night, and after getting it to his shop, he had a chance to look it over. After looking at the intake manifold, he asked if it was ok for him to smooth the porting out a little. Of course! He also wants to pretty up the front covers and the harmonic balancer on the front crank pulley. Why not! I’m sure these will delay the project some more, but I clearly am not making my original goal of a late August debut at Monterey, so I have another year to get everything done.

For now the garage is empty, but for the greasy old Alpina motor.

When wrenching on that, something interesting was discovered. The warm-up regulator bolts to the block (on top of a manifold that has coolant running through it). When unbolting those for Stu to take to Sacramento, we found the bottom of the manifold is exposed to the sump, with a bore through the block and a nice rubber gasket to keep it sealed. Why? What does that accomplish? The m10 K-Jet doesn’t do that and we can’t figure out why the M20 does – so, is it necessary to bore out the new block? We don’t think so, but if you know otherwise, feel free to let me know.

Next up is pulling the Alpina motor apart and figuring out what is in there and whether the head gasket is blown. Then I’ll clean it up and freshen up the innards.

In the meantime, there’s an empty garage space and nature does abhor a vacuum. Will something come up and take that space? An ’02 project? That amazing looking e12 with the S38 on Bring-a-Trailer? An e30 M3? Or will sanity win-out?

Death by a thousand delays

It’s been the far side of two-and-half months since the last post and the motor still hasn’t been completed and the body shell hasn’t really progressed. That’s not to say there hasn’t been progress, but it’s been really slow. Rob Siegel, The Hack Mechanic, counsels that in order to stay connected to a project, you need to do something – something, however small – on it regularly, even if just ordering parts or doing internet research. He says every day. Given my work schedule and life in general, I wasn’t getting the garage much more than once a week. Typically, I go out to the garage, start doing some work and find out I was missing a necessary tool or some part. So not much progress was being made, but I did have plenty of stuff to order and some research to do too! Mostly, there was lots of waiting.

Last we left off, the rotating assembly was installed into the block and it turned smoothly. That was good. To help turn the assembly, I installed the clutch and aluminum flywheel.

Shortly after doing that, I realized I made a bone-headed mistake and didn’t install the rear main seal nor its housing. A legitimate question: How could this happen? The best excuse I have is that I haven’t disassembled the original engine, bought a used block and that part wasn’t included – and then, in all the excitement of getting the rotating assembly together, I simply forgot about such things.

So, the first delay: buy a used housing on eBay and wait for it to arrive; once it does, remove clutch and flywheel, install housing and seal, reinstall clutch and flywheel.

Having never work on an M20 motor before – let alone built one – the next steps vexed me. Unsure of how to tackle it, I started taking the front covers and hubs around the timing belt.

This went smoothly until I encountered the screws securing the intermediate shaft drive. For some reason, instead of using allen screws, BMW used standard head machine screws. Given the torque on these, one simply refused to loosen. Worse, I started to strip the head as I tried. I went into the house, had a beer, and thought about how to get that thing loosened. It came to me: An impact screwdriver!

The second delay: ordering a tool I didn’t have, an impact screwdriver.

Once that arrived, it was simply a matter of a few blows with the mallet, a few more, a couple more for good measure, and the uncooperative screw was beaten into submission, first barely turning but with each blow going a bit further until I was able to remove it with a normal screwdriver. The intermediate shaft drive was off and the new one on! For good measure, new screws holding the drive were ordered and installed, too.

To get to the main pulley the main crank nut had to be removed. Simple concept but considering it’s torqued to more than 300 ft/lbs…. I puzzled on that for a while, since my electric impact wrench wasn’t strong enough. Talked to a few friends, thus further delaying progress.

One friend suggested a piece of 2×4 in the oil sump, preventing rotation and a breaker bar with an extension – in this case the handle from my floor jack. With that long of an extension, the worry is the torque is going to tip the engine stand over, not break the nut. But it worked great; first the nut slowly – very slowly – loosened. And with more movement came more pressure from me. In short order, the nut was off.

Then main pulley had to be removed and that required a puller.

The rest of the front cover removal from the old motor and re-installation on the new one went smoothly.

Next came the oil pump. Wait. Where is the new oil pump? Did I order one? How could I forget that? Couldn’t find one so I searched the invoices for the various parts I ordered. None included an oil pump, so that needed to be ordered. Another delay. While waiting I took the pressure relief valve off the old engine and put it on the new.

Once the oil pump was in hand, I mounted it on the underside of the block. First a test fit, with the drive and then locktite on the bolts. But, since I never worked on an M20 before I didn’t know how the pump (and distributor) was driven. Hence my introduction to the intermediate shaft and the drive off the belt. Some momentum was building, after all the delays, but it was still over a month since the last update here.

The distributor went in.

The head gasket on the block. The head gasket itself is unusual, a metal one that had to be custom made because of the boring out of the block.

The head on that (thanks Frank for the help).

But, wait, where are the washers for the head bolts? Nowhere – not ordered. Another delay. Calls to the local BMW dealers showed none in Northern California, so another parts order and another delay.

Some good progress was made, but it took a long time and had many delays.

Then I had a heart attack (I don’t think it was caused by the delays in the project — more likely genetics and my unhealthy relationship with fatty meats).

That’s the bad news. And that my hope for a big push on the project seems unlikely; that’s also the bad news.

The good news is that after a few days in the hospital I have the time to write up the progress. Oh, and the full recovery prognosis; that’s the good news too.